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Item Prevádzkovo-technické východiská koncepcie BWB letúnov(University of Žilina, 2025) Kováčová, Simona; Škultéty, FilipThe Blended Wing Body is a revolutionary aircraft concept with the potential to surpass present-day conventional aircraft regarding aerodynamic efficiency, and to lower the environmental impact of the aviation industry. However, despite over thirty years of contemporary research, there is still no operational blended wing body airliner, suggesting the presence of multiple unresolved issues pertaining to this design. This article investigates various operational and technical aspects related to the design process of BWB aeroplanes and their influence on the resulting aerodynamic performance. The aim of this work is a multidisciplinary analysis with focus on aircraft structure, operational safety and ultimately on the inter-comparison of required and achievable flight characteristics.Item Optimisation of turboprop aircraft operations as a means to reduce their environmental footprint(University of Zilina, 2021) Števárová, Lucia; Badánik, BenediktThis paper deals with the subject of optimisation of turboprop aircraft operations to decrease their environmental footprint. This aircraft category is not at the forefront of optimisation efforts of operators as it supplies lower volumes of traffic and is equipped with the most fuel-efficient technology for missions served on regional markets. The theoretical part of this paper details turboprop aircraft contributions to global CO2 emissions and analyses aspects behind their efficient performance. Further, it provides a thorough assessment of the operational practices that can significantly reduce the environmental footprint of turboprop aircraft operations. For better illustration, some are exemplified in simple case studies. The practical part of this work aimed to quantify the effects of operational optimisation on turboprop aircraft. Based on the theoretical analysis, we established five operational adjustments whose effects can be determined using performance calculations. These calculations have been carried out using ATR 72-600 aircraft as a reference for a specified average turboprop flight. It was found that through operational adjustments, the fuel consumption on an average ATR 72-600 flight can be decreased on the order of 10%. The energy intensity of operations defined in CO2 per revenue passenger kilometre could be nearly halved compared to actual values of the ATR 72-600 fleet.